Monday, April 26, 2010

Recent Texas Completions and Activity

Completions:
  • Vaughn #4HR, Samson Lone Star: 8.634 MMcf/day IP on 20/64" choke; Carthage (Haynesville Shale) Field, Harrison Co.
  • Hemby GU #3H, NFR Energy: 3.947 MMcf/day IP on 15/64" choke; North Carthage (Bossier Shale) Field, Panola Co.
  • Verhalen "B" #1H, GMX Resources:  2.762 MMcf/day IP on 8/64" choke; North Carthage (Bossier Shale) Field, Harrison Co. (completion data for this well was also reported 11/22/09; I assume one of these entries names the well incorrectly, but I'll report both)
Developmental:
  • Waldron Mary Deep GU #1H, NFR Energy; Carthage (Haynesville Shale) Fiekd, Harrison Co. status #694285
  • George Foreman Gas Unit #1, Samson Lone Star; Carthage (Haynesville Shale) Field, Harrison Co., status #693093
  • Robert Walton #10H, XTO Energy; Carthage (Haynesville Shale) Field, Panola Co., status #694185
  • Williams-Chumley #1H, Devon Energy; Carthage (Haynesville Shale) Field, San Augustine Co. status #694333
  • Tucker #1H, Chesapeake Operating; Carthage (Haynesville Shale) Field, Shelby Co., status #694549
  • Marshall Anderson #1H, EOG Resources; Carthage (Haynesville Shale) Field, Shelby Co., status #694334
  • R. Dean Hay Gas Unit #1H, Goodrich Petroleum; Carthage (Haynesville Shale) Field, Shelby Co., status #694237
  • Beavers DU #1H, XTO Energy; Carthage (Haynesville Shale) Field, Shelby Co., status #694178

2 comments:

Anonymous said...

where did the change in the Devon Energy Whitton 1H IP rate come from?

Robert Hutchinson said...

An error. The 6.65 MMcf/day number is right. I've re-posted the spreadsheet with that fix. My bad - sorry for the confusion.